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How I solved the Tool Offset Problem |
Country Bubba Strikes Again |
In the hobby world, especially with Mill/Drills, we have a problem with tool length offset. This is especially true with the use of R8 collets and many times the use of a chuck to hold drills. Trying to accurately figure and measure length offset and keep it repeatable is a problem. My solution was to re-think the process and come up with a solution that will work for ME! If it helps you, then I am glad to help you. |
Background: My main CNC machine is a RF 31 Mill/Drill which has been modified as shown on other pages to be CNCd with ball screws, Gecko drives and I use TurboCNC as the controller. One of the main "gripes" of a round column mill/drill is the lack of registration when you have to raise/lower the head to accomodate tooling changes. To handle this problem, I set up a "raised table" for those items that would normally be clamped to the table (of course the vice will raise it automatically above the table) and this gives me clearance to change tools. But "calibrating" the length of the tool is very difficult and not very repetive. I installed limit switches on all three axis, and then got to thinking (Very dangerous). First: Convention "Homes" the Z axis to the upper limit. I changed that and home to the lower limit. Thus in G53 (machine fixture), the Z axis is first homed to 0 with NO tool and as such, I know how high I can raise the quill now. Second: I added an "auxiliary" home switch for the Z axis that can be set to the part Z=0 and then using my customized TurboCNC (that can home a single axis under G code), thus enabling me to not only home T0, but also each tool that is inserted. The first aux home switch was made using a micro switch and a lever, proved the concept and was used for a period of time. However, I was afraid the exposed switch would fail in the coolant and swarf environment as it was close to the "action". This was replaced with a commercial switch (as shown below), but even though it was rated at 0.0003" repeatability, it wasn't! Also due to hysterisous I could not reliably set the micro switch by hand as it has a minimum speed at which it should moving when setting. Also, this switch (lever rotary type) has a minimum 25 degree rotation before it would break. Therefore, we now have generation III, an optical switch. Not only does it give greater repeatibility, but only requires a few thou to activate it. Now to the how we have done it. |
This is a shot showing Gen II, the commercial switch doing a homing routine with a tool. The verticle rod is a slide out of a copier and a pre-loaded slide controlled by a knurled knob on the top. With this generation, the switch is set by: 1) Finding the part Z=0 and then putting an led on the switch and raising it until the led goes out and then back down until it just lights. This will (hopefully) be at the part Z=0 (See discussion above) This shot shows the tool at "Home" and while it doesn't look like it, the bar the tool rests on is horizontal at z=0 (important for different diameter tools). However to trip the switch, the lever must go down 25 degrees (about 1 3/8") |
Because of this, we decided to make an optical limit that will only require a few thou move to trip. |
This is a shot of the pieces parts. On the left is a piece of angle with the interrupter mounted. The screw at the bottom is to limit the amount of rotation up for the flag (on the right). Origionally, It was thought that we might need a spring to force the flag down, but it isn't needed. The flag is on the right and includes a ball bearing as the pivot. The notch is to make the assembly horizontal when it trips. |
This show the assembled switch. You can see the stop screw on the left that is needed to keep from rotating to far thus increasing the travel to trip the switch. |
Here, the center drill is being homed using the new optical switch. There are already some changes planned. On is to use a double vertical guid rod as the all-thread rod is not perfectly straight and the tip of the sensor "wobbles" . We also thinking of modification to allow the unit to go lower so we can clamp directly to the table. |
Other ways to help, has been utilize the "Fixture" features of V4.x of TurboCNC. Basically, we use 3 fixtures for our processes. The first is G53 (machine coordinates) which sets the table to the lower left corner as X=0 and Y=0. In all cases (Tool=0), for each fixture. The second G54 is the part fixture and the origin is set accordingly. In the case of the vice fixture, the left end of the fixed jaw is set to 0,0 and we process in Quatrant 2. That is to say that cutting is done in the +X, -Y directions. The third is G59 which I choose to use as the tool change positon. This fixture is chosen as a "free spot" within limits of the table that can home the quill (Tool 0) and have sufficient clear space to allow tool changes (remember this is an R8 quill and needs at least 4 inches to get the collet out! By using "fixtures", it is easy to have my cam program (Sheetcam) simply do the process and then the post is setup to move around as necessary. |
If I can help further, please let me know. |
a_eckstein at bellsouth dot net |
Have a good day, keep smiling AND God Bless America |
In order to set the height of the new limit switch as there is not enough drive from the breakout board to handle another led (it is opto-isolated), we now use the port monitor that is built into TurboCNC. Here, we run the switch up until it opens (as shown on pin 13 which is the Z limit) and then back down until it closes. This will set the Z=0 to the part height. |